After 3 uses, the quadcopter flew away for 1 km and did not return! The reaction to the home button was as follows: after raising the drone by 30-35 meters and moving it 150m away from the take-off point, after pressing the return button, it began to rise more than 110-120m, then manually switching to the mode, I began to lower it, but the copter began to fly away away from me (to the forest) I RUN FOR HIM, but he was faster, in the end, having tried all possible manipulations, I lost the copter . then I tried to find it using the last GPS point and crawling across the field more than one hundred square meters did not find anything .